Ultralight aircraft accidents, experimental aircraft accidents, light sport aircraft accident reports 9 |
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Tower: "Delta Zulu Romeo, turn right now and report your
heading." Pilot: "Wilco. 341, 342, 343, 344, 345..." |
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Ultralight Aircraft Accident Data |
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Witnesses reported that they heard intermittent
engine sounds and observed the airplane descending towards the ground at a steep angle.
Postaccident examination revealed that it had impacted with little forward movement. No
evidence of preimpact airframe anomaly was found. The accident flight was the first flight
after the student pilot/owner/builder converted the engine to a dual ignition/spark plug
system. Examination of the ignition system revealed that the wires going to the magnetic
pickups were pinched between the housing and the crankcase mounting surface, and the wire
insulation was broken. An FAA Inspector stated that the owner/builder had not followed the
manufacturer's recommendation to file a bevel into the edge of the housing during the
ignition system conversion. FAA records indicated that the owner/builder had approximately
30 hours total flight time, and relatives reported that he had not flown the accident
airplane for about two years. Accident occurred MAY-08-95 at CUMMING, GA THE PRIVATE PILOT OBSERVED UNUSUAL ENGINE VIBRATIONS AND NOISE,
AND ELECTED TO PERFORM AN EMERGENCY LANDING IN AN OPEN FIELD. DURING THE LANDING ROLL, THE
RIGHT, MAIN LANDING GEAR STRUCK A HOLE, AND THE GEAR COLLAPSED. AN EXAMINATION OF THE
ENGINE REVEALED THAT ONE OF THE SPARK PLUG LEADS WAS LOOSE. THE AIRCRAFT HAD NOT BEEN
INSPECTED WITHIN THE PREVIOUS 12 MONTHS, AND THE PILOT/OWNER DID NOT POSSESS A CURRENT
BIENNIAL FLIGHT REVIEW OR FAA MEDICAL CERTIFICATE. Accident occurred APR-22-95 at ORLANDO, FL THE PILOT WAS TAXIING AFTER LANDING AND NOTED AN ALLIGATOR TO HIS
LEFT. HE STATED HE ABRUPTLY APPLIED AILERON FLIGHT CONTROL INPUT AND THE RIGHT WING
COLLIDED WITH THE WATER, AND THE AIRPLANE SANK. Accident occurred MAY-02-95 at BRIDGEPORT, MI THE PILOT REPORTED THAT WHILE MAKING A RIGHT CLIMBING TURN AFTER
TAKEOFF, APPROXIMATELY 500 FEET AGL, THE AIRPLANE STARTED TO BANK TO THE LEFT. DESPITE HIS
USE OF FULL RIGHT RUDDER, HE WAS UNABLE TO REGAIN CONTROL. ACCORDING TO THE PILOT,
"THE PLANE KEPT TIGHTENING UP INTO A LEFT FLAT SPIRAL TO THE GROUND." THE
AIRPLANE HAD LEXAN DOORS INSTALLED TO ENCLOSE THE COCKPIT/CABIN AREA. THE DOORS WERE NOT
INCLUDED IN THE ORIGINAL DESIGN OF THIS KIT AIRPLANE, BUT WERE SUBSEQUENTLY MADE AVAILABLE
AS A STANDARD OR OPTIONAL FEATURE, DEPENDING ON THE MODEL. THE MANUFACTURER STATED THAT
WHEN THE DOORS ARE INSTALLED, THE AIRPLANE BECOMES RUDDER DOMINANT AND SENSITIVE AND THAT
PILOTS MUST NOT TAKE THEIR FEET OFF THE RUDDER PEDALS. Accident occurred JUL-09-95 at SILVANA, WA THE PILOT WAS TO PERFORM TWO LOW LEVEL FLY-BYS OVER THE RUNWAY TO
DEMONSTRATE THE QUIETNESS OF THE ENGINE. AFTER THE AIRPLANE MADE THE SECOND PASS, IT
UNEXPECTEDLY DEPARTED THE AREA. WITNESSES OBSERVED THE AIRPLANE FLYING AT A LOW LEVEL,
WHEN THE NOSE OF THE AIRPLANE GRADUALLY LOWERED VERTICAL TO THE TERRAIN AND THE AIRPLANE
BEGAN A SLOW SPIRAL. THE AIRPLANE CONTINUED IN THIS ATTITUDE UNTIL IMPACT. DURING THE
POSTCRASH INSPECTION, NO EVIDENCE WAS FOUND TO INDICATE A MECHANICAL FAILURE OR
MALFUNCTION. THE AIRPLANE'S BALLISTIC RECOVERY SYSTEM HAD NOT BEEN DEPLOYED. Accident occurred APR-07-95 at SUGARTOWN, LA SHORTLY AFTER THE PILOT TOOK OFF FROM HIS PRIVATE AIRSTRIP, THE
ENGINE LOST PARTIAL POWER. HE MADE A SUCCESSFUL FORCED LANDING ON A PRIVATE ROAD. AFTER
CHECKING THE ENGINE AND MAKING A FULL POWER STATIC CHECK, THE PILOT TOOK OFF BUT THE
ENGINE LOST PARTIAL POWER AGAIN. THE PILOT ATTEMPTED TO LAND AT HIS AIRSTRIP, BUT THERE
WAS INSUFFICIENT ALTITUDE AND ENGINE POWER AVAILABLE. THE PILOT MADE A FORCED LANDING IN A
FIELD AND DURING THE LANDING ROLL, THE AIRPLANE NOSED OVER. THE CAUSE OF THE POWER LOSS
WAS NOT DETERMINED. Accident occurred JUN-19-95 at FREEPORT On June 19, 1995, about 1830 EDT, a homebuilt Kolb Twinstar, N5759, registered to Charles T. O'Neill, crashed shortly after takeoff from the Freeport International Airport, Freeport, Bahamas, while on a 14 CFR Part 91 personal flight. Visual meteorological conditions prevailed at the time and a VFR flight plan was filed. The airplane was substantially damaged and the private-rated pilot and one passenger were not injured. The flight originated about 10 minutes earlier. Shortly after takeoff the pilot stated that the engine experienced a loss of power. The airplane collided with terrain about 5 nautical miles southeast of the departure airport. The investigation is under the jurisdiction of the government of the Bahamas. Any further information pertaining to this accident may be obtained from: Director of Civil Aviation, Bahamas P.O. Box N-975 Nassau, N.P. Bahamas Phone: (809) 377-7117 This report is for information purposes only and contains only information released by the Bahamian Government. Accident occurred MAY-03-95 at PHOENIX, AZ THE AIRCRAFT WAS IN THE TAKEOFF INITIAL CLIMB WHEN THE PILOT
DECLARED AN EMERGENCY. THE AIRCRAFT COMPLETED A TURN BACK TOWARD THE RUNWAY, LANDED SHORT
OF THE AIRPORT BOUNDARY, AND STRUCK THE PERIMETER FENCE. THE PILOT REPORTED THAT HE HAD
JUST TAKEN OFF WHEN HE NOTICED THAT THE ENGINE WAS NOT DEVELOPING FULL POWER. JUST THEN,
THE ENGINE QUIT. HE ATTEMPTED TO TURN BACK TOWARD THE RUNWAY BUT DID NOT HAVE SUFFICIENT
ALTITUDE TO REACH THE RUNWAY. A POSTACCIDENT INSPECTION REVEALED THAT THE IGNITION SYSTEM
WAS INOPERATIVE DUE TO A DEFECTIVE DIODE. Accident occurred SEP-08-95 at SCAPPOOSE, OR Witnesses observed the homebuilt aircraft depart from runway 15,
and then they heard the pilot announce his intentions to return to land on runway 33 with
no suggestion of any difficulty. The aircraft was observed to roll off from a turn into a
spin and descend to the ground. An on-site examination revealed no evidence of flight
control or powerplant malfunction. Investigation revealed the aircraft's weight equaled or
exceeded its maximum gross takeoff weight limit. The aircraft was equipped with a recovery
parachute system. The parachute system had been activated, but it had not fully deployed
before ground impact. Accident occurred JUL-08-95 at AUBURN, KS THE PILOT REPORTED THAT HE HAD FLOWN THE AIRCRAFT TWICE IN
NOVEMBER 1994, AND THAT THE AILERONS HAD BEEN "SLUGGISH" AND "SPONGY."
HE HAD NOT FLOWN AGAIN UNTIL THE DAY OF THE ACCIDENT. HE DEPARTED HIS PRIVATE AIRSTRIP AND
"WIGGLED" THE WINGS PASSING 50 FEET. HE FELT THE SAME SLUGGISHNESS THAT HE FELT
THE PREVIOUS NOVEMBER. AT 200 FEET HE REDUCED POWER AND STARTED A 15 DEGREE ANGLE OF BANK
TURN. HE TRIED LEVELING THE WINGS BUT THE AILERONS WERE UNRESPONSIVE AND THE AIRPLANE
CONTINUED TO ROLL. AT 50 FEET HE APPLIED FULL POWER AND RIGHT RUDDER. THE AIRPLANE STRUCK
THE GROUND WITH THE WINGS NEARLY LEVEL. THE PILOT STATED THAT HE MIGHT HAVE REDUCED TOO
MUCH POWER AND GOT TOO SLOW, STALLING THE AIRPLANE. HE HAD NOT FLOWN RECENTLY. HE ALSO
STATED THAT ANOTHER EXPERIENCED PILOT FAMILIAR WITH AN "AVID FLYER" SHOULD HAVE
CHECKED THE FLIGHT CONTROLS BEFORE HE HAD FLOWN THE AIRPLANE AGAIN. Accident occurred JUN-10-95 at KERRVILLE, TX A POTENTIAL BUYER AND 2 FRIENDS (RATED PILOTS) ARRIVED AT THE
AIRPORT FOR A DEMONSTRATION FLIGHT BY THE AIRPLANE DISTRIBUTOR. THE DISTRIBUTOR WAS ALSO
THE OWNER/BUILDER. THE WIND WAS REPORTED TO BE FROM THE EAST-SOUTHEAST AT 15 GUSTING 20
KNOTS. WHEN ASKED ABOUT HOW THE WINDS WOULD AFFECT THE AIRPLANE, THE DISTRIBUTOR STATED
"...NO PROBLEMS." HE OFFERED TO TAKE ONE OF THE RATED PILOTS ON A FLIGHT. DURING
FLIGHT, THE AIRPLANE WAS OBSERVED AT ABOUT TREE TOP HEIGHT, BELOW THE TOP OF HILLS, FLYING
UP A VALLEY FROM THE EAST-SOUTHEAST. THE AIRPLANE WAS OBSERVED TO BANK AND ROLL LEFT WITH
THE WINGS NEAR VERTICAL TO THE GROUND. WITNESSES HEARD ENGINE POWER AS THE AIRPLANE
STARTED DOWN A HILL; HOWEVER, THE AIRPLANE COLLIDED WITH TERRAIN AT THE BOTTOM OF THE
HILL. NO MECHANICAL MALFUNCTION WAS REPORTED NOR FOUND WITH THE ENGINE OR AIRFRAME. THE
AIRPLANE DISTRIBUTOR HELD AN FAA STUDENT PILOT CERTIFICATE. FAR'S REQUIRED AT LEAST A
PRIVATE PILOT CERTIFICATE WITH 200 FLIGHT HOURS FOR A SALES DEMONSTRATION FLIGHT. THE
DISTRIBUTOR HAD NOT REQUESTED THE REQUIRED AIRPLANE INSPECTION BY THE FAA, HAD NOT PAINTED
THE REGISTRATION NUMBER ON THE AIRPLANE, AND HAD NOT BEEN ISSUED AN FAA AIRWORTHINESS
CERTIFICATE. BUILDER RECORDS FOR THE AIRPLANE WERE NOT LOCATED. Accident occurred JUN-22-95 at LONGMONT, CO WITNESSES SAID THE ENGINE LOST POWER SHORTLY AFTER LIFTOFF AT 100
TO 200 FEET ALTITUDE AND THE PILOT BANKED RIGHT IN AN APPARENT ATTEMPT TO MAKE A FORCED
LANDING IN A GRASSY FIELD. ONE WITNESS SAID THE AIRPLANE STALLED AND SPUN BEFORE COLLIDING
WITH TERRAIN. ANOTHER WITNESS OBSERVED PREVIOUS FLIGHTS AND SAID THE ENGINE WOULD LOSE
POWER AFTER TAKEOFF BUT THE PILOT WOULD LAND ON THE REMAINING RUNWAY. ENGINE EXAMINATION
DISCLOSED TIGHT METAL TIES BINDING THE FUEL LINE AGAINST THE STRUCTURE. THE
VACUUM-OPERATED FUEL PUMP WAS MOUNTED ON FLEXIBLE PLASTIC STRIPS, ALLOWING IT TO VIBRATE.
PERSONNEL WHO EXAMINED THE WRECKAGE REPORTED THAT THIS COULD CAUSE THE PUMP TO CAVITATE.
THE PILOT HAD LOGGED 1.6 HOURS IN THE AIRPLANE 10 MONTHS BEFORE THE ACCIDENT. Accident occurred AUG-10-95 at CHINO, CA THE PILOT PERFORMED SOME WORK ON THE ENGINE AND THE PROPELLER AND
ADDED 4 GALLONS OF AUTOMOBILE FUEL TO THE RIGHT TANK PRIOR TO DEPARTURE. AFTER TAKEOFF,
THE PILOT EXPERIENCED A ROUGH RUNNING ENGINE. HE ATTEMPTED A RETURN TO THE AIRPORT BUT THE
ENGINE CONTINUED TO LOSE POWER. DURING THE FORCED LANDING TO AN OPEN FIELD, THE AIRCRAFT
COLLIDED WITH SOME TELEPHONE LINES AND CRASHED INVERTED. THE PILOT DID NOT STATE WHAT THE
SPECIFIC PROBLEM FOR THE LOSS OF POWER WAS. Accident occurred JUN-28-95 at BORGER, TX THE PILOT LANDED AT THE LAKE MEREDITH NATIONAL RECREATION AREA
LOCATED ALONG A RIVER. DURING THE TAKEOFF ROLL FROM THE SOFT UNEVEN TERRAIN WITH TALL
GRASS, THE AIRCRAFT WAS "UNABLE TO BECOME AIRBORNE." THE ONLY PASSENGER EXITED
THE AIRCRAFT. DURING A SECOND ATTEMPTED TAKEOFF, THE AIRCRAFT STRUCK A MOUND OF DIRT AND
"BECAME AIRBORNE AND NOSED DOWN IMPACTING THE GROUND." THE AIRPLANE WAS OBSERVED
"UP TO ABOUT 150 FEET, THEN THE PLANE TOOK A NOSE DIVE." |
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