Ultralight aircraft accidents, experimental aircraft accidents, light sport aircraft accident reports - 10 |
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Tower: "AF1733, You are on an eight mile final for 27RYou have
a UH-1 three miles ahead of you on final; reduce speed to 130 knots." Pilot: "Rogo', Frankfurt. We're bringing this big bird back to one-hundred and thirty knots fer ya." Tower: (a few moments later): "AF33, helicopter traffic at 90 knots now 1 1/2 miles ahead of you; reduce speed further to 110 knots." Pilot: "AF thirty-three reining this here bird back further to 110 knots" Tower: "AF33, you are three miles to touchdown, helicopter traffic now 1 mile ahead of you; reduce speed to 90 knots" Pilot (a little miffed): "Sir, do you know what the stall speed of this here C-130 is?" Tower: "No, but if you ask your co-pilot, he can probably tell you." |
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Ultralight Aircraft Accident Data | |||||
Accident occurred SEP-03-95 at CEDAR
SPRINGS, MI WITNESSES STATED THE HOMEBUILT AIRPLANE'S ENGINE BEGAN SPUTTERING
DURING ITS INITIAL CLIMB AFTER TAKEOFF AND THE AIRPLANE CIRCLED BACK TOWARD THE AIRPORT
FOR A LANDING. DURING ITS APPROACH THE AIRPLANE'S TAIL WHEEL STRUCK A POWER LINE AND THE
AIRPLANE PITCHED DOWN AND COLLIDED WITH THE GROUND. THE ON-SCENE INVESTIGATION REVEALED
CONTROL CABLE CONTINUITY WITH THEIR RESPECTIVE CONTROL SURFACES, AND FOUR FOULED SPARK
PLUGS, TWO THAT HAD NO VISIBLE ELECTRODE GAP. THE PILOT SAID THE PLUGS DIDN'T HAVE TO BE
CLEANED OR CHANGED UNTIL THEY OPERATED FOR 50 HOURS. THE PILOT SAID THE PLUGS HAD BEEN
USED ABOUT 50 HOURS. AN ENGINE MANUFACTURER'S REPRESENTATIVE SAID THE PLUGS NEED TO BE
CHANGED AFTER 25 HOURS OF ENGINE RUNNING TIME. THE REPRESENTATIVE SAID THE ENGINE MUST BE
DECARBONIZED AFTER 50 HOURS OF OPERATION. THE PROCEDURE IS TO INSPECT THE ENGINE AFTER
DISMANTLING THE CYLINDERS, HEADS, AND PISTONS. THE OWNER/PILOT SAID HE CHECKED FOR
CARBONIZATION BY LOOKING IN THE EXHAUST PORT. THE REPRESENTATIVE SAID THIS IS NOT THE
CORRECT PROCEDURE. Accident occurred SEP-02-95 at TEKAMAH, NE THE PILOT REPORTED THAT THE ACCIDENT OCCURRED AT THE CONCLUSION
OF THE SECOND TEST FLIGHT OF N494KN. HE FLEW FOR ABOUT THIRTY MINUTES DOING CONTROL CHECKS
BEFORE RETURNING TO TEKAMAH AIRPORT. WHEN HE TURNED ON THE BASE LEG FOR A FULL STOP
LANDING, THE ENGINE BEGAN RUNNING ROUGH FOR A FEW SECONDS AND THEN STOPPED. HE TRIED TO
RESTART THE ENGINE BUT WAS UNSUCCESSFUL. HE REPORTED THAT HE WAS UNABLE TO MAKE THE RUNWAY
AND MADE AN EMERGENCY LANDING TO A FIELD. THE AIRPLANE HIT A FENCE CAUSING IT TO NOSE
OVER. AN INSPECTION CHECK OF THE AIRPLANE'S SYSTEMS WAS CONDUCTED ON THE FLIGHT CONTROLS,
ENGINE CONTROLS, IGNITION SYSTEM, COOLING SYSTEM, FUEL SYSTEM AND ELECTRICAL SYSTEM. ALL
SYSTEMS APPEARED TO BE OPERATIONAL. A SECOND INSPECTION WAS CONDUCTED TO DETERMINE IF THE
ENGINE WOULD RUN. AFTER THE STARTER WAS REPLACED AND THE WIRING TO THE MAIN FUEL PUMP WAS
REPAIRED, THE ENGINE WAS STARTED AND IT RAN SMOOTHLY. Accident occurred OCT-02-95 at NEWTON, NH DURING THE INITIAL TAKEOFF CLIMB, ABOUT 200 FEET ABOVE GROUND
LEVEL, THE ENGINE LOST TOTAL POWER. THE PILOT PERFORMED A FORCED LANDING, DURING WHICH THE
AIRPLANE COLLIDED WITH TREES AND POWER LINES. THE FAA INSPECTOR STATED THAT DURING THE
POST ACCIDENT EXAMINATION, THE ENGINE WAS SUCCESSFULLY TEST RUN; HOWEVER, "INSPECTION
REVEALED EVIDENCE OF SCORING AND A SMALL AMOUNT OF GALLING ON THE FORWARD CYLINDER
ONLY." Accident occurred OCT-07-95 at COBBS CREEK, VA The pilot stated that the ultralight airplane's performance
appeared normal during the ground roll, liftoff and initial climb. When the airplane was
approximately 130 above the ground, the engine suddenly stopped. The pilot lowered the
nose of the airplane to attain the best glide speed, and made a forced landing in a field.
The airplane struck a tree approximately 40 feet above ground level. Post accident
examination of the engine revealed no evidence of preimpact mechanical malfunction;
however, the spark plug electrodes had a dried deposit on them. The spark plugs were
cleaned and reinstalled, and the engine was satisfactorily test run. Accident occurred OCT-11-95 at NEENAH, WI THE PILOT REPORTED HE WAS CRUISING AT 2000 FEET WHEN THE AIRCRAFT
EXPERIENCED A TOTAL LOSS OF ENGINE POWER. THE AIRCRAFT WAS SUBSTANTIALLY DAMAGED DURING AN
OFF AIRPORT LANDING. AN INVESTIGATION FOUND A FUEL FILTER RETAINING NUT ON THE AUTOMOTIVE
TYPE FUEL FILTER HAD ROTATED CAUSING THE FUEL INLET HOLES TO BECOME BLOCKED. THE
AUTOMOTIVE TYPE FUEL FILTER WAS PURCHASED BY THE AIRCRAFT OWNER FROM A HOMEBUILT AIRCRAFT
PART SUPPLIER. Accident occurred OCT-10-95 at SEMINOLE, TX During the landing roll, the pilot applied right rudder and then
right brake to correct a "slight" left turn. He did not "realize tail was
up so high." The airplane nosed over and came to rest inverted. Accident occurred NOV-13-95 at PLANT CITY, FL The non-rated pilot and a passenger in an unregistered airplane
crashed during takeoff. Witnesses heard the engine running until impact. The airplane was
found where it had impacted in a nose down attitude. Examination of the wreckage revealed
no preimpact failure or malfunction. Accident occurred NOV-20-95 at PASADENA, MD THE PILOT STATED THAT THE AIRPLANE WAS HIGH ON HIS FIRST APPROACH
TO THE 1,700 FOOT LONG GRASS RUNWAY, SO HE PERFORMED A GO-AROUND. HE REPORTED THAT THE
SECOND ATTEMPT WAS GOOD, BUT DURING THE LANDING FLARE, THE AIRPLANE FLOATED, AND TOUCHED
DOWN ABOUT MIDFIELD ON THE RUNWAY. THE PILOT STATED "...I APPLIED BRAKES, BEING
MINDFUL OF THE TREES AT THE END OF THE RUNWAY...THE PLANE NOSED OVER AND FLIPPED ON ITS
BACK." ALSO, THE PILOT REPORTED 21.9 HOURS OF FLIGHT TIME IN THIS MAKE AND MODEL OF
AIRPLANE, OF WHICH ONLY ABOUT 1 HOUR WAS AS PILOT-IN-COMMAND. Accident occurred DEC-16-95 at NEWBERRY, FL Witnesses observed the airplane start a turn towards the north
and then to the west over a state road. The airplane then turned towards the east, banked
to the right, the nose pitch down, and the airplane crashed. The engine appeared to be
running until the airplane collided with the ground. Visual examination of the airframe,
engine assembly and accessories revealed no evidence of a precrash failure or malfunction.
Continuity of the flight control system was confirmed for pitch and roll. The right rudder
cable was attached to the rudder. The left rudder cable was not attached. The attach point
and retainer pin were in place; however, the clevis pin safety ring was missing and later
found by a recovery crew. Safety Board metallurgical examination of the safety ring
revealed features indicative that it was cut. Accident occurred FEB-15-96 at PAHOKEE, FL Witnesses in the area stated that the aircraft was observed to be
practicing maneuvers at about 1000 feet above the terrain. The aircraft appeared to stall
and enter a spin prior to impacting the terrain. Examination of the aircraft, engine, and
related components revealed no evidence of preimpact failure or malfunction. Accident occurred MAR-14-96 at SALUDA, VA The pilot stated that there was a partial loss of engine power
shortly after the airplane lifted off. The airplane would not climb, so he elected to land
on the remaining runway. In his attempt to avoid lights at the end of the runway, the
pilot stalled the airplane approximately ten feet above the surface. The airplane impacted
the runway in a steep nose down attitude, then "...rolled over onto it's back."
Postaccident investigation revealed that the #1 spark plug failed an electrical function
test. The pilot stated that the spark plug operated normally under low load conditions,
but "...[stopped] under full load." Accident occurred FEB-09-96 at GRANTSVILLE, UT While in a climb over the south end of the Great Salt Lake, the
engine oil temperature reached the upper limit (red line). The pilot reduced power and
monitored the oil temperature while proceeding to the southwest shoreline of the lake.
After passing over the shoreline, the pilot started looking for a place where he could
land to investigate the cause of the problem. He elected to land in an open snow-covered
field, which had snow that he estimated was 1 to 3 inches deep. After a successful
touchdown, the aircraft rolled about 60 feet, and then flipped over in the snow. After the
accident, the pilot determined that the snow was actually 6 to 8 inches deep. Accident occurred MAY-05-96 at TALKEETNA, AK The pilot was in cruise flight on a personal flight when he noted
a rise in the rear cylinder head temperature of the number two (rear) cylinder. He
adjusted the mixture screw and watched the temperature continue to rise. During a
precautionary landing, the engine stopped producing power, and the pilot was forced to
land the airplane on a road. Subsequent examination showed that the piston in the rear
cylinder would not move. Examination of the mixture screws showed that the mixture screw
controlling the rear cylinder was in the lean position. The direction on rotation for
leaning or enriching the mixture was not marked on the mixture screws. Accident occurred APR-06-96 at SALEM, OR The non-certificated pilot, who was flying an unregistered
homebuilt aircraft, experienced a complete power loss during the climb after departure. He
successfully maneuvered the aircraft to an open field for an emergency landing; however,
as he began the landing flare, he allowed the airspeed to get low. The aircraft then
stall/mushed into the terrain with enough force to result in substantial damage to the
airframe. After the accident, no reason for the power loss could be found, and the engine
operated successfully during a test run. The aircraft was similar to an ultralight, but
its empty weight and fuel capacity exceeded the limits for it to be classified as an
ultralight. Accident occurred JAN-27-96 at OMAHA, NE During landing the airplane veered left and could not be
corrected. The airplane then impacted a snowbank on the side of the runway and nosed over.
The left wheel fairing was found completely packed with snow. Once the snow was removed
the wheel rotated freely. The pilot stated that the snow apparently had accumulated in the
wheel fairing when he taxied through snow drifts earlier prior to departing the North
Omaha airport for Denison. While landing at Denison, the airplane had pulled to the right.
During the return trip to the North Omaha airport, the pilot realized that his left brake
was probably frozen, and decided to divert to the Eppley Airfield because of the wider
runway there. Accident occurred MAY-26-96 at BRIDGEPORT, AL The pilot stated that the engine lost power during cruise flight.
He then attempted a forced landing. During the forced landing, the right wing collided
with a tree, and the airplane was damaged. No reason was found for the loss of engine
power. Accident occurred JUL-17-96 at TENAKEE SPRINGS, AK The pilot was landing on a remote lake in a float-equipped
homebuilt airplane toward the east in calm wind conditions. After touchdown, the pilot
retracted the flaperons, slowed to about 20 miles per hour, and was settling off the float
step. A gust of wind struck the left side of the airplane and tilted the right wing down.
The right wingtip contacted the water and the airplane rolled up onto the front of the
right float assembly. The airplane then nosed over. Accident occurred JUN-01-96 at INDEPENDENCE, OR The pilot reported that just after takeoff, at an
altitude of 40 to 50 feet above ground level, and at an indicated airspeed of 35 MPH,
"the nose and left wing pitched up and started to roll to the right." The pilot
attempted to counteract with "forward left stick." He stated that the nose then
lowered, but the right roll continued. The aircraft impacted the ground right wing first.
Information supplied with the pilot's accident report listed the airplane's maximum gross
weight as 725 pounds and its stall speed as 30 MPH. The pilot supplied a gross weight
computation with his accident report, indicating an actual aircraft gross weight of 727
pounds before takeoff. The pilot used a pilot weight for this computation which was 12
pounds lower than the weight given on his FAA medical certificate. The pilot indicated on
his accident report that no mechanical malfunction or failure was involved. |
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